WANG Zhe. Application of controllable shock wave plugging removal and permeability improvement technology in CBM gas field of Southern Yanchuan[J]. Petroleum Reservoir Evaluation and Development, 2020, 10(4): 87-92.DOI:
In order to solve the problems such as coal blockage and low gas production of coalbed methane wells in the Southern Yanchuan block
an application test of controlled shock wave plugging removal and permeability improvement technology is carried out. Therefore
four typical wells are selected to analyze the geological and engineering parameters in the construction process
as well as comparative analysis of the gas and water production before and after the implementation. The results show that the application of controllable shock wave plugging removal and permeability improvement technology in coalbed methane wells can improve liquid fluidity
promote gas desorption and diffusion
and remove plugging in coal reservoirs. The well selection criteria of this technology are low coalbed fracture pressure
good fracturing effect
including dirt band
high gas-bearing capacity of coalbed
relatively high formation pressure coefficient
etc. This technology has the effect of creating fractures and removing plugs
which can improve the fluidity of formation fluids and remove formation pollution. It has a good implementation effect and application prospect in the near-well zone of south Yanchuan coalbed methane wells to plugging removal and increase gas production
and is expected to be a new stimulation technology for low yield and efficiency wells.