Technical countermeasures for deep pumping of highly deviated wells in deep reservoir
- Issue 2, Pages: 247-253(2023)
Published:2023
DOI: 10.13809/j.cnki.cn32-1825/te.2023.02.014
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Published:2023
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南堡油田地处滩海,油井位置局限,整体开发以大斜度定向井为主,受油藏形成特性影响,断块发育破碎,横向面积小,纵向含油层系多,低能量区存在大量供液不足的油井,泵的常规下入深度难以满足连续生产的供排需求,导致单井效益过低,同时泵筒充不满加剧了井下杆柱应力的复杂性和偏磨程度。在对抽油机井杆管泵进行综合分析的基础上,提出了深抽工艺的技术对策,并由油藏压力和生产参数预测了深抽放大压差的增产潜力,从多级杆柱加深后应力计算及延长生产周期等配套工艺技术研究入手,通过软件模拟深抽后杆柱应力变化,对深抽后不同深度杆柱进行应力测试与理论计算对比,并对相关配套工艺进行优化设计,确保深抽后杆柱应力的安全性。实现了深抽后油井动液面下降,产能增加,沉没度的增加
并提高了泵筒充满系数,泵挂深度平均加深800 m、最大泵挂深度达到3 300 m,生产压差平均放大6 MPa,泵效平均提高10个百分点,单井增油平均提高300 t,同时针对不同油层物性、不同供液能力的油井进行效果分析和经验总结,形成了不同油井深抽的可行性评价方法。
Nanpu Oilfield is located in the tidal sea with limited oil well spacing
and the overall development is dominated by highly oblique directional wells. Due to the characteristics of reservoir formation
the fault blocks are developed and broken
and the transverse area is small
the longitudinal layer distribution is large
and there are many oil wells with insufficient liquid supply in the low energy area. The conventional pump running depth is difficult to meet the supply and drainage requirements of continuous production
resulting in low efficiency of a single well. At the same time
the dissatisfaction of the pump barrel aggravates the complexity and eccentric wear degree of the down-hole rod stress. Based on the comprehensive evaluation of the rod
pipe and pump of the pumping unit system
the technical countermeasures of deep pumping are put forward. And the stimulation potential of deep pumping amplified pressure difference is predicted by the reservoir pressure and production parameters. The stress calculation after multi-stage rod deepening and the extension of production cycle are studied. After the simulation of the stress change of the rod column after deep pumping by the software
the stress test and theoretical calculation of the rod column at different depths after deep pumping are compared
and the related supporting technology is optimized to ensure the stress safety of the rod column after deep pumping. After deep pumping
the oil well dynamic fluid level decreased and the productivity increased. The increase of subduction reduced the filling dissatisfaction of the pump barrel. The setting depth of the pump is deepened averagely by 800 meters and can reach a depth of 3 300 meters. The production pressure difference
the pump efficiency
and the single well oil increment increase by 6 MPa
ten percentage points and 300 tons respectively on average. At the same time
the effect analysis and experience summary are carried out for oil wells with different reservoir properties and different liquid supply capacity
and the feasibility evaluation method of deep pumping in different oil wells is formed.
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